Design Improvement of a Helicopter Tail Reducer Casing

The helicopter tail reducer casing often fail in the process of development. A design improvement scheme of a helicopter tail reducer casing is proposed based on the test results of the applied full stress monitoring method. The full stress monitoring method contains static test,fatigue test,ground...

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Main Authors: Guo Tiancai, Mei Qing, Xue Tongbo, Huang Zhenrong
Format: Article
Language:zho
Published: Editorial Office of Journal of Mechanical Transmission 2016-01-01
Series:Jixie chuandong
Subjects:
Online Access:http://www.jxcd.net.cn/thesisDetails#10.16578/j.issn.1004.2539.2016.07.041
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author Guo Tiancai
Mei Qing
Xue Tongbo
Huang Zhenrong
author_facet Guo Tiancai
Mei Qing
Xue Tongbo
Huang Zhenrong
author_sort Guo Tiancai
collection DOAJ
description The helicopter tail reducer casing often fail in the process of development. A design improvement scheme of a helicopter tail reducer casing is proposed based on the test results of the applied full stress monitoring method. The full stress monitoring method contains static test,fatigue test,ground test and flight test. The static and fatigue weak position of the casing is exposed by the static test and fatigue test. Through the ground test and the flight test,it is found that the main cause of failure is the resonance between the casing and system. According to the above test results,the design improvement scheme is proposed. The main contents are as follows,changing the connecting strength of the reinforcing plate of the foot,reducing the thickness of the lightening hole in the ribbed plate area,increasing the thickness of the install foot,increasing the thickness of install side of the pinion roller bearing. The above local changes make the casing well matched with the system,meanwhile the stress is redistributed to improve its fatigue and static property. The dynamic stress level of the casing is reduced by 49%after improvement. The quality is significant increased by the ground test and the flight test.
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spelling doaj.art-f9da1ab6b5cd4285946bef87a99029a32023-05-26T09:41:40ZzhoEditorial Office of Journal of Mechanical TransmissionJixie chuandong1004-25392016-01-014018819129925146Design Improvement of a Helicopter Tail Reducer CasingGuo TiancaiMei QingXue TongboHuang ZhenrongThe helicopter tail reducer casing often fail in the process of development. A design improvement scheme of a helicopter tail reducer casing is proposed based on the test results of the applied full stress monitoring method. The full stress monitoring method contains static test,fatigue test,ground test and flight test. The static and fatigue weak position of the casing is exposed by the static test and fatigue test. Through the ground test and the flight test,it is found that the main cause of failure is the resonance between the casing and system. According to the above test results,the design improvement scheme is proposed. The main contents are as follows,changing the connecting strength of the reinforcing plate of the foot,reducing the thickness of the lightening hole in the ribbed plate area,increasing the thickness of the install foot,increasing the thickness of install side of the pinion roller bearing. The above local changes make the casing well matched with the system,meanwhile the stress is redistributed to improve its fatigue and static property. The dynamic stress level of the casing is reduced by 49%after improvement. The quality is significant increased by the ground test and the flight test.http://www.jxcd.net.cn/thesisDetails#10.16578/j.issn.1004.2539.2016.07.041Tail reducer;Fault diagnosis;Stress monitoring;Static test;Fatigue test
spellingShingle Guo Tiancai
Mei Qing
Xue Tongbo
Huang Zhenrong
Design Improvement of a Helicopter Tail Reducer Casing
Jixie chuandong
Tail reducer;Fault diagnosis;Stress monitoring;Static test;Fatigue test
title Design Improvement of a Helicopter Tail Reducer Casing
title_full Design Improvement of a Helicopter Tail Reducer Casing
title_fullStr Design Improvement of a Helicopter Tail Reducer Casing
title_full_unstemmed Design Improvement of a Helicopter Tail Reducer Casing
title_short Design Improvement of a Helicopter Tail Reducer Casing
title_sort design improvement of a helicopter tail reducer casing
topic Tail reducer;Fault diagnosis;Stress monitoring;Static test;Fatigue test
url http://www.jxcd.net.cn/thesisDetails#10.16578/j.issn.1004.2539.2016.07.041
work_keys_str_mv AT guotiancai designimprovementofahelicoptertailreducercasing
AT meiqing designimprovementofahelicoptertailreducercasing
AT xuetongbo designimprovementofahelicoptertailreducercasing
AT huangzhenrong designimprovementofahelicoptertailreducercasing