Stalled flow performance of a single stage transonic compressor

Originally presented as the first author's thesis, M.S. in the M.I.T. Dept. of Mechanical Engineering, 1978

Bibliographic Details
Main Authors: Bartlett, Frederick Girard, Greitzer, E. M. (Edward M.), 1941-
Other Authors: Massachusetts Institute of Technology. Gas Turbine and Plasma Dynamics Laboratory
Format: Technical Report
Published: Cambridge, Mass. : Massachusetts Institute of Technology, Gas Turbine & Plasma Dynamics Laboratory, [1978] 2016
Subjects:
Online Access:http://hdl.handle.net/1721.1/104421
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author Bartlett, Frederick Girard
Greitzer, E. M. (Edward M.), 1941-
author2 Massachusetts Institute of Technology. Gas Turbine and Plasma Dynamics Laboratory
author_facet Massachusetts Institute of Technology. Gas Turbine and Plasma Dynamics Laboratory
Bartlett, Frederick Girard
Greitzer, E. M. (Edward M.), 1941-
author_sort Bartlett, Frederick Girard
collection MIT
description Originally presented as the first author's thesis, M.S. in the M.I.T. Dept. of Mechanical Engineering, 1978
first_indexed 2024-09-23T16:51:17Z
format Technical Report
id mit-1721.1/104421
institution Massachusetts Institute of Technology
last_indexed 2024-09-23T16:51:17Z
publishDate 2016
publisher Cambridge, Mass. : Massachusetts Institute of Technology, Gas Turbine & Plasma Dynamics Laboratory, [1978]
record_format dspace
spelling mit-1721.1/1044212019-04-12T16:13:20Z Stalled flow performance of a single stage transonic compressor Bartlett, Frederick Girard Greitzer, E. M. (Edward M.), 1941- Massachusetts Institute of Technology. Gas Turbine and Plasma Dynamics Laboratory TJ778.M41 G24 no.144 Compressors -- Aerodynamics Aerodynamics, Transonic Originally presented as the first author's thesis, M.S. in the M.I.T. Dept. of Mechanical Engineering, 1978 Includes bibliographical references (page 48) The stalled flow performance of a single stage transonic compressor is examined, using data from the MIT Gas Turbine Laboratory's Blowdown Compressor Facility. Measurements of the blowdown corrected weightflow are included, as well as stage exit static to inlet total pressure rise, and rotating stall cell measurements. A comparison of the flow blockage, as represented by stall cell circumferential extent, with the blowdown corrected weightflow is made. The 100% design speed stalled flow performance characteristic is presented. Radial traverse.data is also presented including flow angles, static and total pressures, and Mach number components. Supported by the NASA Lewis Research Center grant NGL 22-009-383 2016-09-27T19:59:06Z 2016-09-27T19:59:06Z 1978 Technical Report http://hdl.handle.net/1721.1/104421 06550418 GT & PDL report ; no. 144 79 pages application/pdf Cambridge, Mass. : Massachusetts Institute of Technology, Gas Turbine & Plasma Dynamics Laboratory, [1978]
spellingShingle TJ778.M41 G24 no.144
Compressors -- Aerodynamics
Aerodynamics, Transonic
Bartlett, Frederick Girard
Greitzer, E. M. (Edward M.), 1941-
Stalled flow performance of a single stage transonic compressor
title Stalled flow performance of a single stage transonic compressor
title_full Stalled flow performance of a single stage transonic compressor
title_fullStr Stalled flow performance of a single stage transonic compressor
title_full_unstemmed Stalled flow performance of a single stage transonic compressor
title_short Stalled flow performance of a single stage transonic compressor
title_sort stalled flow performance of a single stage transonic compressor
topic TJ778.M41 G24 no.144
Compressors -- Aerodynamics
Aerodynamics, Transonic
url http://hdl.handle.net/1721.1/104421
work_keys_str_mv AT bartlettfrederickgirard stalledflowperformanceofasinglestagetransoniccompressor
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