A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.

Massachusetts Institute of Technology. Dept. of Aeronautics and Astronautics. Thesis. 1967. M.S.

Bibliographic Details
Main Author: Shaw, John, Jr
Other Authors: Rene H. Miller.
Format: Thesis
Language:eng
Published: Massachusetts Institute of Technology 2014
Subjects:
Online Access:http://hdl.handle.net/1721.1/86252
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author Shaw, John, Jr
author2 Rene H. Miller.
author_facet Rene H. Miller.
Shaw, John, Jr
author_sort Shaw, John, Jr
collection MIT
description Massachusetts Institute of Technology. Dept. of Aeronautics and Astronautics. Thesis. 1967. M.S.
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spelling mit-1721.1/862522019-04-10T09:03:40Z A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control. Shaw, John, Jr Rene H. Miller. Massachusetts Institute of Technology. Department of Aeronautics and Astronautics Aeronautics and Astronautics Massachusetts Institute of Technology. Dept. of Aeronautics and Astronautics. Thesis. 1967. M.S. Microfiche copy available in Barker. Bibliography: leaves 95-96. M.S. 2014-04-25T15:46:45Z 2014-04-25T15:46:45Z 1967 Thesis http://hdl.handle.net/1721.1/86252 24013424 eng M.I.T. theses are protected by copyright. They may be viewed from this source for any purpose, but reproduction or distribution in any format is prohibited without written permission. See provided URL for inquiries about permission. http://dspace.mit.edu/handle/1721.1/7582 ix, 96 leaves application/pdf Massachusetts Institute of Technology
spellingShingle Aeronautics and Astronautics
Shaw, John, Jr
A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.
title A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.
title_full A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.
title_fullStr A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.
title_full_unstemmed A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.
title_short A feasibility study of helicopter vibration reduction by self-optimizing higher harmonic blade pitch control.
title_sort feasibility study of helicopter vibration reduction by self optimizing higher harmonic blade pitch control
topic Aeronautics and Astronautics
url http://hdl.handle.net/1721.1/86252
work_keys_str_mv AT shawjohnjr afeasibilitystudyofhelicoptervibrationreductionbyselfoptimizinghigherharmonicbladepitchcontrol
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