ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)

System Identification is a method for determining the dynamic model of a system from input and output measurements of the system. Knowing a model system is needed to design and implement control systems with optimal performance. System identification is an experimental approach for determining the d...

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Main Authors: , HARDY FERRYSIAN LOGIANI, , Dr.-Ing. Awang N I Wardana dan Dr. Ir. Andang Widi Harto ,M.T.
Format: Thesis
Published: [Yogyakarta] : Universitas Gadjah Mada 2014
Subjects:
ETD
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author , HARDY FERRYSIAN LOGIANI
, Dr.-Ing. Awang N I Wardana dan Dr. Ir. Andang Widi Harto ,M.T.
author_facet , HARDY FERRYSIAN LOGIANI
, Dr.-Ing. Awang N I Wardana dan Dr. Ir. Andang Widi Harto ,M.T.
author_sort , HARDY FERRYSIAN LOGIANI
collection UGM
description System Identification is a method for determining the dynamic model of a system from input and output measurements of the system. Knowing a model system is needed to design and implement control systems with optimal performance. System identification is an experimental approach for determining the dynamic model of a system. Based on the results of closed-loop identification with algorithm closed-loop output error (CLOE) condenser system plant model is obtained and the control valve is of second order system. Analysis of responses transient and steady state of model in a closed loop system with exciting controller in the plant showed a fast oscillating with a settling time 4.28 seconds, peak time 3.58 seconds, rise time 0.756 seconds and no error steady state. Re-tuning control system gives the best results in response system using proportional-integral controller (PI) with the principle of ISE. The aim of re-tuning is to find the controllers constant that provides optimum performance and gives safety of the system especially in the actuator and the final element. Simulation results using MATLAB software shows the settling time of 24.7 seconds, peak time 3.57 seconds, rise time of 1.03 seconds and no steady state error occured. Controller constants the results of the re-tuning proportional band (K) is 260.34%, integral time (Ti) is 0.36 seconds and the time derivative (Td) 0 seconds.
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institution Universiti Gadjah Mada
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spelling oai:generic.eprints.org:1273942016-03-04T07:56:45Z https://repository.ugm.ac.id/127394/ ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG) , HARDY FERRYSIAN LOGIANI , Dr.-Ing. Awang N I Wardana dan Dr. Ir. Andang Widi Harto ,M.T. ETD System Identification is a method for determining the dynamic model of a system from input and output measurements of the system. Knowing a model system is needed to design and implement control systems with optimal performance. System identification is an experimental approach for determining the dynamic model of a system. Based on the results of closed-loop identification with algorithm closed-loop output error (CLOE) condenser system plant model is obtained and the control valve is of second order system. Analysis of responses transient and steady state of model in a closed loop system with exciting controller in the plant showed a fast oscillating with a settling time 4.28 seconds, peak time 3.58 seconds, rise time 0.756 seconds and no error steady state. Re-tuning control system gives the best results in response system using proportional-integral controller (PI) with the principle of ISE. The aim of re-tuning is to find the controllers constant that provides optimum performance and gives safety of the system especially in the actuator and the final element. Simulation results using MATLAB software shows the settling time of 24.7 seconds, peak time 3.57 seconds, rise time of 1.03 seconds and no steady state error occured. Controller constants the results of the re-tuning proportional band (K) is 260.34%, integral time (Ti) is 0.36 seconds and the time derivative (Td) 0 seconds. [Yogyakarta] : Universitas Gadjah Mada 2014 Thesis NonPeerReviewed , HARDY FERRYSIAN LOGIANI and , Dr.-Ing. Awang N I Wardana dan Dr. Ir. Andang Widi Harto ,M.T. (2014) ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG). UNSPECIFIED thesis, UNSPECIFIED. http://etd.ugm.ac.id/index.php?mod=penelitian_detail&sub=PenelitianDetail&act=view&typ=html&buku_id=67645
spellingShingle ETD
, HARDY FERRYSIAN LOGIANI
, Dr.-Ing. Awang N I Wardana dan Dr. Ir. Andang Widi Harto ,M.T.
ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)
title ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)
title_full ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)
title_fullStr ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)
title_full_unstemmed ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)
title_short ANALISIS KINERJA SISTEM PENGENDALI LEVEL DI CONDENSER DENGAN IDENTIFIKASI SISTEM KALANG TERTUTUP (STUDI KASUS DI CONDENSER PEMBANGKIT LISTRIK TENAGA PANAS BUMI UNIT IV PT.PERTAMINA GEOTHERMAL ENERGY AREA KAMOJANG)
title_sort analisis kinerja sistem pengendali level di condenser dengan identifikasi sistem kalang tertutup studi kasus di condenser pembangkit listrik tenaga panas bumi unit iv pt pertamina geothermal energy area kamojang
topic ETD
work_keys_str_mv AT hardyferrysianlogiani analisiskinerjasistempengendalileveldicondenserdenganidentifikasisistemkalangtertutupstudikasusdicondenserpembangkitlistriktenagapanasbumiunitivptpertaminageothermalenergyareakamojang
AT dringawangniwardanadandrirandangwidihartomt analisiskinerjasistempengendalileveldicondenserdenganidentifikasisistemkalangtertutupstudikasusdicondenserpembangkitlistriktenagapanasbumiunitivptpertaminageothermalenergyareakamojang